It is not a precise adjustment.
It can be 2, 2 1/2, or whatever, as long as it idles smoothly.
It can be 2, 2 1/2, or whatever, as long as it idles smoothly.
These are a little lean at the factory..2 and a half out will not cause runability problems in itself.As mentioned in another thread this bike when brought to me for help wouldn't start, there was a smell of gas but would not run.
Things I've discovered, plugs black and wet, battery sitting on foam block covering openings to intake airbox, stock mufflers removed and replaced with HD Sportster items, exhaust valves adjusted too tight.
To remedy those things I've installed new plugs, removed the foam block which leaves the intake snorkel unrestricted, new owner has purchased a used set of stock take off exhaust for the EN500 (yet to arrive and install), valve clearances checked and adjusted per spec.
Last night I pulled the carbs, disassembled, inspected and cleaned them. Actually they were very clean inside, all passages clear.
Someone had removed the caps over the pilot air screw and the screws were adjusted to 2 1/2 turns out from seated. Per service manual they should be 2 1/8 turns out. Additionally I found a small flat washer under the flange on the main jet needle which would raise it slightly. There's no washer in the illustration of the carb breakdown that I could see.
Should I remove the washer and set the air screw per spec?
I would assume that more turns out on the air screw and raising the main jet needle richen the mixture?
Thanks